中国科学院机构知识库网格
Chinese Academy of Sciences Institutional Repositories Grid
Cause investigation and verification of lining cracking of bifurcation tunnel at Huizhou Pumped Storage Power Station

文献类型:期刊论文

作者Xiao, Ming2; Bian, Kang1; Liu, Jian1; Liu, Zhenping1
刊名TUNNELLING AND UNDERGROUND SPACE TECHNOLOGY
出版日期2016
卷号54页码:123-134
关键词Lining cracking Bifurcation tunnel Insufficient thickness Numerical simulation Cause investigation
ISSN号0886-7798
DOI10.1016/j.tust.2015.10.030
英文摘要A wide range of cracking happens in concrete lining at the crown of the lower adit and high-pressure bifurcation in the water-filled test of bifurcation tunnel at Huizhou Pumped Storage Power Station. Then a field investigation is undertaken to explore the main reason of such prominent lining cracking. Through investigating several possible inducing factors, it is found that mass defects exist in the concrete lining in constructing bifurcation tunnel, and insufficient thickness of concrete lining is probably the main factor causing lining cracks. In order to verify if this conclusion is reasonable, comparative analysis through numerical simulation is utilized to assess the influence of different concrete thicknesses on tunnel stability for the lower adit and high-pressure bifurcation. And then the fracturing process of concrete lining with the increase of internal water pressure during the water-filled test is simulated. The results reveal that the displacements and tensile strains in the lining crown are significantly bigger than other parts of tunnel, with deficiency in concrete thickness considered. It is also concluded that whether the cavities exist or not in the crown, rather than the cavity thickness, is the main factor influencing the values and distributions of the tensile strains and displacements for tunnel lining. Besides, the distribution of tensile-strain-concentrated zones is approximately in good agreement with the in-situ fractured status of concrete lining. Finally, a conclusion can be drawn that deficiency in concrete thickness in the crown is the primary triggering factor for lining cracking. (C) 2015 Elsevier Ltd. All rights reserved.
WOS研究方向Construction & Building Technology ; Engineering
语种英语
WOS记录号WOS:000372679400013
出版者PERGAMON-ELSEVIER SCIENCE LTD
源URL[http://119.78.100.198/handle/2S6PX9GI/3849]  
专题岩土力学所知识全产出_期刊论文
国家重点实验室知识产出_期刊论文
作者单位1.Chinese Acad Sci, State Key Lab Geomech & Geotech Engn, Inst Rock & Soil Mech ;
2.Wuhan Univ, State Key Lab Water Resources & Hydropower Engn S
推荐引用方式
GB/T 7714
Xiao, Ming,Bian, Kang,Liu, Jian,et al. Cause investigation and verification of lining cracking of bifurcation tunnel at Huizhou Pumped Storage Power Station[J]. TUNNELLING AND UNDERGROUND SPACE TECHNOLOGY,2016,54:123-134.
APA Xiao, Ming,Bian, Kang,Liu, Jian,&Liu, Zhenping.(2016).Cause investigation and verification of lining cracking of bifurcation tunnel at Huizhou Pumped Storage Power Station.TUNNELLING AND UNDERGROUND SPACE TECHNOLOGY,54,123-134.
MLA Xiao, Ming,et al."Cause investigation and verification of lining cracking of bifurcation tunnel at Huizhou Pumped Storage Power Station".TUNNELLING AND UNDERGROUND SPACE TECHNOLOGY 54(2016):123-134.

入库方式: OAI收割

来源:武汉岩土力学研究所

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