中国科学院机构知识库网格
Chinese Academy of Sciences Institutional Repositories Grid
Study on Sealing Failure of Wellbore in Bedded Salt Cavern Gas Storage

文献类型:期刊论文

作者Chen, Xiangsheng; Li, Yinping; Liu, Wei; Ma, Hongling; Ma, Jianli; Shi, Xilin; Yang, Chunhe
刊名ROCK MECHANICS AND ROCK ENGINEERING
出版日期2019
卷号52期号:1页码:215-228
关键词Bedded salt cavern storage Wellbore tightness test Leaking mudstone interlayer Permeability Leakage analysis
ISSN号0723-2632
DOI10.1007/s00603-018-1571-5
英文摘要The wellbore tightness of a salt cavern gas storage must be tested before solution mining. According to the test results, it will be evaluated whether the wellbore can meet the cementing requirements of gas storage. However, there are many complex reasons that may cause wellbore leakage; hence, how to comprehensively analyze the test results and accurately expose the causes, locations, and scale of the leakage pose many challenges. These mainly include the incomplete test method and lack of theoretical analysis model. A nitrogen leak test was carried out for five wellbores that have been completed in Jintan (Jiangsu, China). The results show that two of them had leakage risk. To clarify the leakage causes and leakage types, we carried out an investigation of engineering geological data of the wellbores and further conducted laboratorial tests and theoretical analysis. The studies of drilling design and engineering geology show that the wellbores have good integrity and initially reveal that a mudstone interlayer intersecting the open hole between the casing shoe and the top of the salt cavern is a potential leaking layer. Furthermore, the permeability experiments and CT scans confirm that this mudstone interlayer is a leaking stratum and that the internal cracks develop severely. They are the key reasons leading to wellbore tightness failure. The proposed seepage theoretical model determines that the leakage type is horizontal flow in the mudstone interlayer. Comparing the theoretical results with the field test data, we find that the leakage rate curves of the two are in good agreement, which completely confirms that the mudstone interlayer is the fundamental cause of the wellbores tightness failure. This research not only identifies the leakage causes and leakage types of wellbores, but also enriches the leakage rate analysis method of gas storage and provides a theoretical and experimental analysis method for tightness evaluation of bedded salt cavern storage.
WOS研究方向Engineering ; Geology
语种英语
WOS记录号WOS:000456673000014
源URL[http://119.78.100.198/handle/2S6PX9GI/15095]  
专题岩土力学所知识全产出_期刊论文
国家重点实验室知识产出_期刊论文
作者单位1.Univ Chinese Acad Sci, Beijing 100000, Peoples R China;
2.Chinese Acad Sci, Inst Rock & Soil Mech, State Key Lab Geomech & Geotech Engn, Wuhan 430071, Peoples R China;
3.Chongqing Univ, State Key Lab Coal Mine Disaster & Control, Chongqing 400044, Peoples R China
推荐引用方式
GB/T 7714
Chen, Xiangsheng,Li, Yinping,Liu, Wei,et al. Study on Sealing Failure of Wellbore in Bedded Salt Cavern Gas Storage[J]. ROCK MECHANICS AND ROCK ENGINEERING,2019,52(1):215-228.
APA Chen, Xiangsheng.,Li, Yinping.,Liu, Wei.,Ma, Hongling.,Ma, Jianli.,...&Yang, Chunhe.(2019).Study on Sealing Failure of Wellbore in Bedded Salt Cavern Gas Storage.ROCK MECHANICS AND ROCK ENGINEERING,52(1),215-228.
MLA Chen, Xiangsheng,et al."Study on Sealing Failure of Wellbore in Bedded Salt Cavern Gas Storage".ROCK MECHANICS AND ROCK ENGINEERING 52.1(2019):215-228.

入库方式: OAI收割

来源:武汉岩土力学研究所

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