中国科学院机构知识库网格
Chinese Academy of Sciences Institutional Repositories Grid
Long-term uplift of high-speed railway subgrade caused by swelling effect of red-bed mudstone: case study in Southwest China

文献类型:期刊论文

作者Dai, Zhangjun2; Guo, Jianhua1,2; Yu, Fei2; Zhou, Zhe1,2; Li, Jian2; Chen, Shanxiong2
刊名BULLETIN OF ENGINEERING GEOLOGY AND THE ENVIRONMENT
出版日期2021-03-26
页码15
ISSN号1435-9529
关键词High-speed railway Subgrade Long-term uplift Red-bed mudstone Swelling
DOI10.1007/s10064-021-02220-7
英文摘要A high-speed railway must support fast-moving vehicles and have strict low-deformation requirements. However, many high-speed railways encounter the problem of abnormal subgrade deformation caused by expansive rocks. In this study, the Neijiangbei station of the Chengdu-Chongqing high-speed railway in Southwest China, where the subgrade has undergone continuous and stable uplift during the construction and operation periods, was considered as an example. The Jurassic red-bed mudstone widely distributed in this area is a typical expansive rock, and its swelling effect is the main cause behind the uplift of the subgrade. Results of water-absorption tests, disintegration tests, and expansion tests indicate that the red-bed mudstone is characterized by easy disintegration, slow water absorption, and long-term swelling. A decoupling analysis method for the seepage and swelling of red-bed mudstone was proposed to simulate the water infiltration through the fissures and the temporal and spatial changes in the swelling. Using monitoring data, an inversion analysis of the high-speed railway subgrade uplift was conducted, and the subgrade deformation was predicted. The results suggest that the main changed area of the moisture-content field in the rock formation was a small area near the fissure layer. The moisture content of the mudstone increased rapidly in the first few years of infiltration and increased slowly over subsequent decades. Correspondingly, the subgrade uplift increased rapidly in the first few years after excavation owing to the swelling of the mudstone; thereafter, the growth rate decreased, but the subgrade uplift maintained long-term continuous growth for several decades.
资助项目National Natural Science Foundation of China[41702337] ; National Natural Science Foundation of China[51579236]
WOS研究方向Engineering ; Geology
语种英语
出版者SPRINGER HEIDELBERG
WOS记录号WOS:000633287400003
源URL[http://119.78.100.198/handle/2S6PX9GI/25974]  
专题中科院武汉岩土力学所
通讯作者Dai, Zhangjun
作者单位1.Univ Chinese Acad Sci, Beijing 100049, Peoples R China
2.Chinese Acad Sci, Inst Rock & Soil Mech, State Key Lab Geomech & Geotech Engn, Wuhan 430071, Peoples R China
推荐引用方式
GB/T 7714
Dai, Zhangjun,Guo, Jianhua,Yu, Fei,et al. Long-term uplift of high-speed railway subgrade caused by swelling effect of red-bed mudstone: case study in Southwest China[J]. BULLETIN OF ENGINEERING GEOLOGY AND THE ENVIRONMENT,2021:15.
APA Dai, Zhangjun,Guo, Jianhua,Yu, Fei,Zhou, Zhe,Li, Jian,&Chen, Shanxiong.(2021).Long-term uplift of high-speed railway subgrade caused by swelling effect of red-bed mudstone: case study in Southwest China.BULLETIN OF ENGINEERING GEOLOGY AND THE ENVIRONMENT,15.
MLA Dai, Zhangjun,et al."Long-term uplift of high-speed railway subgrade caused by swelling effect of red-bed mudstone: case study in Southwest China".BULLETIN OF ENGINEERING GEOLOGY AND THE ENVIRONMENT (2021):15.

入库方式: OAI收割

来源:武汉岩土力学研究所

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